Post by tr1ppler on Dec 14, 2018 9:42:52 GMT -5
So I have a penchant to go down roads to "Save money" that end up costing me more money but I also like doing things the hard way. So this is a realization of those two tendancies
A big part of me working on this bike is to learn as much as I can. This is the first bike I've actually dug into the motor at all past the valve cover, I've painted a bunch of bits, I'm trying to learn whatever I can, and part of that is the next step. Rewinding the stator.
The good news. The field coil tested okay. Didn't ground to the core and had 4.9 ohms of resistance from lead to lead.
So I tested the 3 legs of the stator and instead of 0.7 ohms on each leg of the triangle, as expected, I got 24, 27, and 6 ohms. So not close.
Also based on the burned out stator connector and the signs of an exploded battery all over the exhaust I think this is the reason the bike was parked in the first place. That history is 3 owners past so I'm trying to piece it together forensically.
Could I buy one on eBay? Yes. 2 reasons why I am not doing this.
1) I am not entirely sure that the "new" stator would be a lot better
2) I'm in this to learn what I can
So before jumping off the cliff, I thought I should do some due diligence.
So I opened it up and tore off all of the old white silicone that was used to seal off the wire passages by one of the POs.
I took out the field coil because I could not see that there are 2 bullet connectors that allow you to leave it in the side cover when you remove the stator and wiring. They were covered in the white silicone.
I thought I would try and test the 3 wires at the stator end to see if the bad resistance was coming from the harness itself. The fabric wire sleeves were pure carbon and broke up if touched, taking the wires with them. So now I was officially huptey-juped, I was very successful at ensuring I had to rebuild this whole thing by accidentally breaking it.
The good news (sort of) is that testing the leads to the union of the 3 wires confirmed that the wires in the stator themselves are bad. I got these three results:
5.3 ohms
22 ohms
0.7 ohms
So one of the 3 legs is good. One is bad. One is terrible. So at least I don't have to rebuild it because I broke the wires but because the wraps are bad. This stator is Delta wound which means the 3 legs junction at one place.
So after the initial inspection, I found that the wire looks to be 19 gauge. I'm thinking of rewrapping with 18 gauge and seeing if I can put in a few extra turns to increase the output. I'm no electrical engineer and haven't found anything that I totally understand yet, so those decisions are still forthcoming.
Next step is to unwind the current stator to look at the wrap pattern and see how much magnet wire I will need.
A big part of me working on this bike is to learn as much as I can. This is the first bike I've actually dug into the motor at all past the valve cover, I've painted a bunch of bits, I'm trying to learn whatever I can, and part of that is the next step. Rewinding the stator.
The good news. The field coil tested okay. Didn't ground to the core and had 4.9 ohms of resistance from lead to lead.
So I tested the 3 legs of the stator and instead of 0.7 ohms on each leg of the triangle, as expected, I got 24, 27, and 6 ohms. So not close.
Also based on the burned out stator connector and the signs of an exploded battery all over the exhaust I think this is the reason the bike was parked in the first place. That history is 3 owners past so I'm trying to piece it together forensically.
Could I buy one on eBay? Yes. 2 reasons why I am not doing this.
1) I am not entirely sure that the "new" stator would be a lot better
2) I'm in this to learn what I can
So before jumping off the cliff, I thought I should do some due diligence.
So I opened it up and tore off all of the old white silicone that was used to seal off the wire passages by one of the POs.
I took out the field coil because I could not see that there are 2 bullet connectors that allow you to leave it in the side cover when you remove the stator and wiring. They were covered in the white silicone.
I thought I would try and test the 3 wires at the stator end to see if the bad resistance was coming from the harness itself. The fabric wire sleeves were pure carbon and broke up if touched, taking the wires with them. So now I was officially huptey-juped, I was very successful at ensuring I had to rebuild this whole thing by accidentally breaking it.
The good news (sort of) is that testing the leads to the union of the 3 wires confirmed that the wires in the stator themselves are bad. I got these three results:
5.3 ohms
22 ohms
0.7 ohms
So one of the 3 legs is good. One is bad. One is terrible. So at least I don't have to rebuild it because I broke the wires but because the wraps are bad. This stator is Delta wound which means the 3 legs junction at one place.
So after the initial inspection, I found that the wire looks to be 19 gauge. I'm thinking of rewrapping with 18 gauge and seeing if I can put in a few extra turns to increase the output. I'm no electrical engineer and haven't found anything that I totally understand yet, so those decisions are still forthcoming.
Next step is to unwind the current stator to look at the wrap pattern and see how much magnet wire I will need.